Air India Fuel Switch Checks Confirm Safety, Boeing Procedure Followed

The Ministry of Civil Aviation stated that inspections of an Air India Boeing 787's fuel control switches found them to be operating satisfactorily within specified limits. The checks, performed in the presence of DGCA officials, followed Boeing's recommended procedures after a crew reported a latching concern during engine start in London. The ministry clarified that a viral social media video demonstrated an incorrect method for operating the switch. The airline has been advised to circulate the correct Boeing procedure to its crew members.

Key Points: Air India Fuel Switch Found OK, Boeing Procedure Correct

  • Fuel switches passed Boeing checks
  • Social media video showed wrong procedure
  • Flight completed safely in Bengaluru
  • DGCA officials oversaw inspections
3 min read

Air India plane's fuel control switches found to be okay: Civil Aviation Ministry

Civil Aviation Ministry clarifies Air India B787 fuel control switch was satisfactory after checks. Social media video used incorrect procedure.

"Both left and right switches were checked and found satisfactory - Civil Aviation Ministry"

New Delhi, Feb 3

The Ministry of Civil Aviation on Tuesday issued a rejoinder on the news item relating to the purported malfunction of the fuel cut-off switch on Air India's Boeing B787-8 aircraft VT-ANX in London.

The rejoinder states that, based on the Boeing recommended checks to establish the serviceability of the fuel control switch, Air India engineering observed that: "Both left and right switches were checked and found satisfactory, with the locking tooth fully seated and not slipping from RUN to CUTOFF. When full force was applied parallel to the base plate, the switch remained secure. However, applying external force in an incorrect direction caused the switch to move easily from RUN to CUTOFF, due to the angular base plate allowing slip when pressed improperly with finger or thumb."

In addition, based on Boeing's communication, the pull-to-unlock force was checked on the fuel control switch using the recommended procedure on the involved fuel cut-off switch, the fuel control unit to be installed, and the fuel cut-off switch of another aircraft. In all cases, the pull-to-unlock force was found within limits. These inspections were carried out in the presence of DGCA officers, the ministry's statement said.

The video currently circulating on social media was analysed in light of Boeing's recommended procedures, and it was observed that the procedure demonstrated in the video being circulated is incorrect, the statement observed.

The airline is being advised to circulate the Boeing recommended procedure for the operation of the Fuel CUT OFF switch to its crew members, the statement said.

On February 1, 2026, Air India B787-8 aircraft VT-ANX operated flight AI 132 (London- Bengaluru). During engine start in London, on two occasions, the crew observed that the fuel control switch did not remain positively latched in the 'RUN' position when light vertical pressure was applied. On the third attempt, the switch latched correctly in 'RUN' and subsequently remained stable. Before continuing with the rest of the procedure, a physical verification was performed by the crew to confirm that the switch was fully and positively latched in the 'RUN' position. No abnormal engine parameters, cautions, warnings, or related system messages were observed during engine start or at any time thereafter.

The operating crew member was briefed on the observation, unnecessary contact with the switch was avoided, and engine indications and alerting systems were closely monitored by the crew for the remainder of the flight. The flight was completed without incident.

After landing at Bengaluru, the crew reported the defect in the PDR. Air India referred the matter to Boeing for further guidance, after which the airline's engineering department carried out the checks in the presence of DGCA officials, the statement said.

- IANS

Share this article:

Reader Comments

P
Priya S
This is a relief! I fly Air India often for work between Delhi and Bangalore. The crew handled it professionally, and the follow-up with Boeing shows proper protocol. Hope the training for all crew on the correct procedure happens quickly.
R
Rohit P
While the final report says the switches are okay, the initial incident where it didn't latch twice is concerning. Boeing's design seems tricky if pressing it "incorrectly" makes it slip so easily. They should look into a more foolproof mechanism.
S
Sarah B
As an expat living in Bengaluru, I appreciate the transparency in this statement. It's detailed and addresses the viral video directly. The crew's caution and monitoring during the flight is commendable.
V
Vikram M
The key takeaway is the procedure in the viral video was wrong. This is why we shouldn't jump to conclusions based on social media posts. Air India engineering and DGCA did the right thing by involving Boeing and following their checks.
K
Kavya N
I have a respectful criticism. The ministry's rejoinder is good, but it came after the video spread widely. In today's age, our aviation authorities need to be faster with their official communications to prevent misinformation from settling in.
M
Michael C
Technical issues happen with complex machinery. What matters is the response. Here,

We welcome thoughtful discussions from our readers. Please keep comments respectful and on-topic.

Leave a Comment

Minimum 50 characters 0/50